Seeing how I don’t really have a feasible way to test the injectors, I have a spare set of injectors, so I swapped in a replacement into #4 port. Initial start up was leaps and bounds better. These are the readings, after noticing there was finally heat on the #4 primary tube. Issue solved!
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Last edited by '68 C10; 10-02-2018 at 09:30 PM.
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